Well, finally got to the bottom of my heat problem. New thermostat helped alot. Still getting some off the wall temps out of the blue though. Turns out that my return line going to my degas bottle wasnt sealing. Would puke out all my coolant with 0 pressure in the tank. Guess it was like riding around with no cap on. So, last night after I figured all of this out, I hooked a pressure gauge up and went for a ride. Everything looked good. No puking, no weird temps. Right up until I pulled on it past 3/4 throttle.:doh: Gauge pegged 16 psi.. Whoops!!LOLLOL So, now it looks like I will pulling it again for the umpteenth time. Wont be anytime soon though. Im tired of working on it for a while. Think I will just let it be leaky. If it gives up the ghost, oh well. Swap something else into it. Im not mad at it though. Ive given this thing HELL!!!! I really figured the tranny would have cut loose first. Think I will buy a few parts here and there and maybe get around to it towards the end of the summer. My work schedule doesn't leave me with much free time. So it looks like I have joined the ranks of the blown HG gang!!LOLLOLLOL
When I go back in, will throw some more goodies at it!
Tuned 58v FICM
Reg Return
Oil bypass
New water pump
Oil cooler
Inter cooler
Have to see what all the check book says about it. Might do some cosmetics as well.
When I go back in, will throw some more goodies at it!
Tuned 58v FICM
Reg Return
Oil bypass
New water pump
Oil cooler
Inter cooler
Have to see what all the check book says about it. Might do some cosmetics as well.
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