Forums
New posts
Search forums
What's new
New posts
New media
New media comments
New profile posts
Latest activity
New showcase items
New showcase comments
Media
New media
New comments
Search media
Members
Current visitors
New profile posts
Search profile posts
Showcase
New items
New comments
Latest content
Latest reviews
Latest updates
Search showcase
Log in
Register
What's new
Search
Search
Search titles only
By:
New posts
Search forums
Menu
Log in
Register
Install the app
Install
Forums
Non - Specific
Engine Conversion
07 expedition gets 4bta'd
JavaScript is disabled. For a better experience, please enable JavaScript in your browser before proceeding.
You are using an out of date browser. It may not display this or other websites correctly.
You should upgrade or use an
alternative browser
.
Reply to thread
Message
[QUOTE="gwunter, post: 1367931, member: 9742"] The old girl is still up and running. Actually better than ever. After the hx30 install it just didnt seem to run right for some reason. And i finally figured it out. It seemed to have a miss feeling during higher rpm and heavy load. I checked everything i could easily check and was stumped on it ever since the hx30 install. I never hooked up my ksb cold start mechanism on the injection pump, which was in turn advancing my injection timing 5*!! I never hooked it up because it always started so well. But i still cant explain why i didnt notice this miss type feeling with the h1c. But now it runs really well and pull in the upper rpms better. When i was testing it after the ksb hookup, the boost went to 45psi!! I was shocked it did tgat. The waste gate was closed off. Ill need to get my waste gate controlled better as i beliece 45psi is way off its map....and i dont want it to eat a compressor or chuck a turbine. I have also swapped out the luk clutch for a spec stage 3.5 clutch.there is a night and day difference in these clutches. Im very impressed with the clutch. Nice smooth action and good engagement. Ive also purchased ford factory service manuals to straighten out some creature comfort issues. Compounds, innercooler, and better amsoil oil filter setup are still to come. Im also going to install a air fuel ratio gauge to better tune the IP, pyro is installed and running and she never breaks 1200*f yet. Its got some smoke down low i would like to get rid of. [/QUOTE]
Insert quotes…
Verification
Post reply
Random media
Latest posts
10R140 failure
Latest: PSD-BLACK-CLOUD
Yesterday at 1:04 PM
2017+ 6.7 Aluminum Super Duty
2010 headunit
Latest: glog
Wednesday at 1:17 PM
6.4 Tech
D
Turning off the Auxiliary powertrain control module
Latest: donaldtfreeman
Tuesday at 10:43 AM
6.0 Tech & FAQ
4r100 P0715/P0717 trouble codes.
Latest: Tiha
Tuesday at 8:07 AM
7.3 Tech & FAQ
I must be getting old… Exhaust is too loud
Latest: ju015dd
Sunday at 7:59 AM
6.0 Aftermarket
Members online
Jacobzek
Christianzek
Forums
Non - Specific
Engine Conversion
07 expedition gets 4bta'd
Top