50_shooter
Member
noooo built bottom end blew the first one smh.
What setup did you blow the original bottom with? Was it bent rods?
noooo built bottom end blew the first one smh.
If all works out over the next week I'll be swapping out my 13 pump for a 15 and still keep the H&S Dual Fuel pump. I'm not gaining only a few HP going over 2300us and if the 15 pump alone does 647 this should easily be able to push me across 700 wheel HP.
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That turbo won't be happy for long at 50+ boost. Might try a swap to a 1.0 turbine housing or gate it
Are you going to start making them all like that Mike? (Rolled lip)
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Not a problem. Cut 1-1/8" out of the pipe and welded back together and now we have a perfect fit. I was able to make several test runs over the weekend and never had any problems with the hoses or connections coming off even at peek boost at 53lbs.
Everything has come together and I think we are finished with this setup.
Could not be happier with the results of the 367FMW. Ended up with 12.6 1/4 with 671HP in Craig's Race tune. My daily driver Tune settings are 615/627/643 HP and the mileage is not bad. I have seen over 17 @ 70mph on a trip if I drive very conservative on flat ground in FL. I tow quite a bit with a trailer that weighs more than 17,000lbs. Tows real well and is very clean.
Next step will be the 69mm Turbo if it comes out. Until then I will work on my 60ft times and tire pressures with the 420's to see if we can do better. Possible a OUO 4 link to stop the dancing at the line.
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Have you had any problem with your truck defueling and coming up on the display "exhaust filter over limit, service now" AFTER delete? If so, what did you do to fix it?