6.4 Stroker
Member
Take the nozzle off the injector from the failed hole. Just about bet you the nozzle is clogged.
I hope you do in fact find something in the injectors. However, attached is what my piston looked like. Mine showed a melted whole as well as a crack across the piston.
I as well, suspecting a bad injector, sent all 8 to RCD. they tested and flowed them to find nothing wrong.
Sorry about the large rotated images, not sure how to fix them.
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Where yall running a hopped up tune that caused these piston issues or stock trucks
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As sootie said, I think this happens stock or tuned. My truck went at on a diet at 9k and smoked a piston at 128k. Never skipped a beat until that day. And I never took it off a performance setting or ran it hotter than 1300deg.Where yall running a hopped up tune that caused these piston issues or stock trucks
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And the cause being emissions over fueling, excessive heat from egr, or what. Hopped up to me is 150+ above stock, i run a tow tune most of the time but have put the 100 hp tume on it occasionally....runs well but i worry about it...dont do street "racing" around
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Ahhh yes good point. My thinking of .010 is .020 total. If you don't mind me asking, what was the approximate cost of the new block from Ford?
Where yall running a hopped up tune that caused these piston issues or stock trucks
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Ouch..... Was that exchange? No need for the bill, that gives me a ball park. It just keeps sucking up funds every time I turn around. Why the heck do these have to cost so dang much for every little (or big) piece.